神东矿区1.8 m以下采高综采装备效率提升研究

    Study on efficiency enhancement of fully mechanized mining equipment with mining height below 1.8 m in Shendong Mining Area

    • 摘要: 针对神东矿区1.8 m以下中厚偏薄煤层综采装备效率低的问题,通过对寸草塔煤矿31109综采工作面生产现场跟踪写实和数据分析,得出采煤机与刮板输送机间的过煤间隙偏小是制约开采效率主要原因。提出了提高采煤机机身高度、提高截割电机位置、加大截割深度和推移步距三种解决措施。分析改造费用和生产能力计算表明,通过加大截割深度和推移步距因改造费用高昂,不建议改造;通过适当提高采煤机机身高度和截割电机位置,可提升该工作面22%的开采效率,具备改造实施价值,为神东矿区中厚偏薄煤层综采成套设备高效开采技术研究提供了很好的借签意义。

       

      Abstract: To address the low efficiency of fully mechanized mining equipment for medium-thin coal seams with mining heights below 1.8 meters in Shendong Mining Area, field tracking and data analysis are conducted at the 31109 fully mechanized mining working face of Cuncaota Coal Mine. The results indicate that the insufficient clearance between the shearer and the scraper conveyor is the primary constraint on mining efficiency. Three improvement measures are proposed: increasing the shearer body height, elevating the cutting motor position, and enhancing cutting depth and advancing step distance. Cost-benefit analysis of retrofitting and production capacity calculations shows that increasing cutting depth and advancing step distance are not recommended due to high retrofitting costs. However, moderately raising the shearer body height and cutting motor position could improve the mining efficiency of the working face by 22%, demonstrating viable retrofitting potential. This study provides valuable insights for the research on high-efficiency mining technologies for fully mechanized mining equipment in Shendong’s medium-thin coal seams.

       

    /

    返回文章
    返回